Improved Defrost Cycle for Heat Pump Systems
and Comparisons of heating systems for Moderate Climates (like Georgia)
by Joe Mehaffey
Rev 13, July 12, 2012 (added new graphic)
A new heat pump defrost control cycle
is described which is shown to dramatically reduce the number of
defrost cycles needed by heat pumps in the author's environment.
The costs involved in this control cycle implementation if done
on a production basis would probably be less than $25 which would be
easily recovered in less than one year of operation.
Some Preliminary Information
In the summer of 2007, I installed a
Carrier Heat Pump for a client in the Atlanta, Georgia area. This
changeout was designed to improve
the efficiency of the heating and cooling equipment. The 25HNA9
heat pump was a 48000btuh unit with SEER rated 19 and a COP in heating
mode of about 3 at 27F and about 4 at 37F. As an example, this
means that for a total input of about 3.3KW (equivalent to about
10,800btuh) at 34F, the heating system outputs about 40,000btuh into the
building. According to Carrier data, at a temperature of 37F, the cost per therm of
heat (100,000btu) is about 2.5x 3.3KWH =8.25KWH. Here
in Georgia, the "all up" cost per KWH on the residential TOU rate
in winter is about 8cents per kwh. So the cost to move 1 Therm of
heat from outside (37F) to the inside of the house is about 8.25kwh x
8cents per KWH = $0.66 at a nominal outside temperature of 37F. This compares to about $1.50 per therm as
an "all up" cost per therm for Natural Gas (95% efficiency furnace).
For fuel oil at about $2.50 per gallon you get about 140,000btu
per gallon and with a 90% efficiency Oil Furnace the cost
per therm is about $1.98 per therm. Similarly for electric RESISTANCE
heat which is often used as supplemental heat for heat pumps, the cost
per therm is again about 8cents per KWH and you get 3413 btuh per KWH. Thus
100,000btuh will cost (100000/3413) x 8c = $2.35 per therm.
In summary, with the SEER =19/COP = 4 (at T=37F) heat pumps available now
AND with a reasonable electric energy cost such as we have here in Georgia, the obvious solution
for home heating is a heat pump with whatever backup heat
(NG/Propane/Fuel Oil/Electric) that is best for your area. NOTE:
Heat pumps WILL NOT be as efficient in colder northern climates,
so you must run a calculation similar to the above to determine costs in your area at various temperatures.
With the above in mind, we installed the heat pump system and an adjunct
high efficiency (SEER=17) Air Conditioner and the client enjoyed a summer with
about a 25% lower overall electric energy cost compared to that using the older SEER 12 air conditioners. Cheers!
The Carrier 25HNA9 48,000btuh "Ultra" Heat Pump System.
This Heat pump system is a LITTLE unusual. The unit was purchased with the thinking that it would be rather simple to
connect it up to the existing furnace and zoned control system.
What a surprise when I opened the manual and it said, "This
equipment can only be used with Carrier Furnaces and Infinity
Thermostats".. After mulling things over for a day, we found that
there were no readily available air source heat pump systems with the
efficiency of the one we had bought. So... Since I am an
Electrical Engineer by trade, we set about to figure out WHY this
heat pump could not be used with "ordinary" furnaces. The answer
was: A marketing decision was made to integrate the furnace, heat
pump, thermostats and zones so that they would "talk" only over a pair of
wires. I am sure that somewhere along the way, the marketeers
figured this was a good way to force anyone wanting Carrier's premium
heat pump product to "Go Carrier All The Way". I think that
perhaps this is a great marketing strategy for Carrier and it
eliminates any potential equipment compatibility problems and allows
certain system optimizations as well.
BUT!.. I wanted to use the 25HNA9048 heat pump with the existing 12
year old stainless firebox 95% efficiency Amana Furnace. The
installed Building Automation System is a system designed and manufactured by HI Solutions Inc. The system was designed for use in
LARGE commercial buildings but it uses a distributed architecture that
makes it quite adaptable (by an HVAC Engineer) and cost effective to use for buildings of any
size, including medium to large sized homes. Since this
system was already up and running in the home and grounds, we chose
the HI Solutions model UUC-8 Universal Controller to REPLACE the Carrier Heat Pump
Controller Card inside the heat pump. This meant we had to adapt
the basic heat pump to operate with the new UUC-8 controller AND
program this controller so it could both control and protect the heat
pump and also communicate and interface with the remainder of the
building automation system. This process took several days. I was able to procure product
literature from Carrier which described in some detail how their
controller functioned and I simply wrote a 40 line program for the UUC-8 universal controller (in a
language similar to BASIC) to operate and monitor the heat pump equipment.
While I was at it, I added a few
instrumentation "niceties" so we could
monitor the detailed performance of the heat pump from my remote
computers. The UUC-8 controller has 8 Analog Inputs, 12
Switch Closure Inputs, 3 Analog Outputs, and 8 ports with Triac
Switchable 24vac at up to 2 amps. I set up the new UUC-8
controller to control
the scroll compressor, reversing solenoid, and the High/Low
capacity solenoid in
the heat pumpcompressor unit itself. Then we added a
"furnace run
(enable GAS)" signal, a furnace Fan High/Low signal, an overall
FURNACE ENABLE signal, and a Heat Pump/Furnace select signal. The
technician built a simple relay tree interface for the furnace end so
that any single
wire or signal failure could not put the furnace (or the heat pump) in
RUN and leave it there. As an added safety feature, a
standard Honeywell thermostat was connected in series with the
furnace system's gas valve so that if return air
ever gets over 80F, the gas valve in the furnace cannot be turned on.
On a "one of a kind" system such as this, MULTIPLE safeguards are
an essential ingredient because "errors happen" and you do not want a
small "program error" to overheat your client's house!! One of
the analog
outputs go to control the GE variable speed fan in the heat pump unit,
Analog input sensors monitor Outside Air temperature,
Evaporator refrigerant OUTLET
temperature, and Suction Line temp on the line coming from the
furnace evaporator/condenser. UUC-8 switch closure inputs include
Puron OverPressure, Puron Under Pressure, plus an input from the
furnace air vane switch which proves furnace air flow. (The
compressor is never allowed to run unless air flow in the connected
furnace air handler is "proved".).
Then a current transformer was added so as to be able
to monitor
heat pump compressor and outside fan unit current draw.
This, along with the other data
available in the UUC-8 allows the computation of a good quality
estimate of the system SEER, COP, and to allow the program to
monitor for overcurrent, overtemperature, overpressure and various
other abnormal conditions as may arise.
What about the DEFROST CYCLE is so interesting?
In November, North Georgia weather turned rather
cool. Night low temperatures were going from 27F to about 45F
which has allowed a good laboratory for getting the heat pump right down
to freezing for a few hours and then quickly bringing the temperature
into the 50 to 70 range in the daytime. During this interval, I
noticed via the remote instrumentation that the heat pump was going into defrost mode in the 3am to
8am
time period but we found that the defrosts were producing little water. I was
basically using Carrier's defrost algorithm which goes like this:
You power up and the system resets the defrost interval to a value of 30
minutes of compressor running time in heating mode. Then, after
this 30 minutes expires, the temperature of the evaporator refrigerant outlet line is
measured and if it is less than 32F a defrost cycle is initiated.
Then, when a defrost cycle is initiated, if the time it
takes to defrost the outside
evaporator coil (as evidenced by the outside coil exhaust temperature
being greater than 65F) is less than 3 minutes, the next defrost
interval is set to 120 minutes, if between 3 and 5 minutes set
the defrost
interval to 90 minutes, if between 5 and 7 minutes, set the
defrost interval to 60 minutes, and if it takes greater than 7 minutes
to defrost the evaporator, set the next defrost interval to 30 minutes.
The decision to defrost (or not) is that AFTER the compressor
runs for the defrost interval, check the outside coil refrigerant
outlet temperature. If it is below 32F, then defrost, if not,
reset the timer and continue operations. This algorithm leads to
unneeded defrost cycles where the coil is really NOT iced up to an
extent affecting efficiency in a significant way.
We noticed that a good many
defrosts (1 to 3 a day) produced little
water from the defrost cycle. I was a bit curious as to the
"real" amount of
ice being developed and so we temporarily disabled the defrost part of
the program but left in a "freeze up shutoff" if the coil temperature
ever got down to 15F. The equipment was watched
remotely for another week and the outside
refrigerant outlet temperature never got lower than 22F and never
differed from the outside air temperature by more than about 8 degrees.
(Did I mention that the UUC-8 also has trend logging for analog
and digital inputs and most any internal variable you may wish to log
for later review? The log comes complete with a date/time stamp.)
In this case, we logged what would have been defrost cycles.
There were 19 in a 10 day period but NOT ONE was actually needed.
I decided that there had
to be a better way to determine WHEN to defrost so as not to waste the
energy used in the defrost cycle. A typical defrost cycle lasts
about 4 minutes and pumps "cool" air into the house and warms up the
outside evaporator thus causing any ice to melt. Then when the
heat pump is reversed back to heating mode, it takes LONGER to
pump the
heat back into the house than the defrost cycle took. All in all
you are "defrosting and getting back where you were" to the tune
of maybe 10 minutes or more for each defrost cycle. The energy used is in
the range of 3KW (at 33F) for 1/6 hour or about 4 cents per
defrost. This is not a great deal of money per cycle, but
you ALSO lose the
heat pump capacity for that 10 minutes which amounts to perhaps 7000btu
for the average defrost cycle. Note that even more energy is used for the
defrost cycle when electric heat is used to compensate for the cooling
effect in the home due to the defrost cycle. In fact, a defrost cycle
compensated by electric heat will cost about 9 cents for each defrost cycle..
Another reason for wanting to
try and optimize the defrost cycle
was to try to be able to operate the heat pump at lower temperatures
than the 30 or so degrees typical of these systems. While the
heat output goes down significantly below 30F, the heating
capacity is still substantial. This 48000btu HP system capacity is
approximated by the formula BTU OUTPUT = 1000(0.63T+17). Where T
is the outside air temperature in degrees F. This equipment is
rated to
produce HALF its rated capacity at about 15F. Though this BTU
output will likely be inadequate to maintain comfort, even
at 0F, the cost per therm is less using the heat pump than that cost
using Natural Gas or any of the other optional fuels. In this
setup, we are
able to use the 48,000BTU/H Natural Gas furnace simultaneously with the 48,000 BTU/H heat pump
as needed since the two furnaces share a common plenum system which
feeds the entire home. The furnace serving as air handler for the Heat Pump is a 90,000BTU NG Amana unit.
Now to the discuss the new DEFROST CYCLE implementation
As an example of what the new defrost
scheme can do, see Figure 10 (below) where the heat pump was run at
temperatures between 20F and 30F for 12 hours and required ZERO defrost
cycles.
We gave a lot of thought about
options for deciding when a defrost was needed. In the end,
it seemed to me that "freezing up"
would be accompanied by a reduced air flow produced by the heat pump
outdoor unit fan. This reduced air flow would be
accompanied
by a reduced air pressure (vacuum) inside the heat pump fan/evaporator
enclosure. We installed a 0-1 inch differential air pressure
transducer inside the heat pump enclosure for experiments. The
low pressure
side connected by rubber tube through a hole to the inside of the
heat pump enclosure and the high pressure side was led by a similar
tube
to a place exterior to the enclosure. Tubes were installed so it
was downhill from the transducer to prevent rain from entering
the tube and running into the transducer. With this transducer
and other measurement tools, we discovered that, over another
week,
the
Carrier algorithm wanted to defrost 14 times and my algorithm wanted to
defrost once. During this interval, I allowed NO defrosts and at
no time did the evaporator inlet/outlet differential temperature
exceed 9F (except during system startup). The "ice free"
differential air pressure across the coil is nominally 0.11 inches.
On just one occasion during the week long test, the
differential air pressure drop across the coil
got up to 0.4". Based on this (rather sparse) data, I have
initially set up the defrost algorithm with a) NO timers, but
instead, b) the
algorithm is programmed to defrost the system whenever the air pressure
drop exceeds 0.37" -or- if the "evaporator input to evaporator
output" refrigerant temp
differential across
the coil exceeds 15F. The differential temperature
(Outside Air minus Evaporator Coil Outlet Temperature) is allowed to
excursion to 25F for up to 10 minutes following a startup. This
transient on startup is normal and does not call for a defrost.
The above defrost scheme (in this moderate weather) is definitely doing a
much more frugal job of handling system defrost and without any
apparent reduction in efficiency. In fact, due to fewer defrost
cycles, the system's overall efficiency is increased by maybe 2
to 3 % plus a similar increase in system heating capacity due to fewer
defrost cycles.
As the winter gets colder and the data folder gets thicker, I am
certain to have refinements to the above scheme.. Stay Tuned!
Below is the client's Building Automation System's Main Floor Display. Note
the extensive instrumentation of the HVAC equipment in the Top-Upper
Right. Special data display for the heat pump experiments include
Defrost OFF/ON, delta-T across the liquid inlet to vapor outlet of the
outside evaporator, Fan Speed, VACuum (x100) across the outside evaporator,
HPbtuh for given OAT, computed from balance curves furnished by
Carrier, Heat Pump Amps, computed instantaneous SEER for heat pump,
Heat Pump Ambient(OAT), HP-OCT (HP outside coil outlet temp, Inside HP
condenser INPUT air temp (BYPT), HP supply side (heated) air temp,
Duct Supply Pressure, Furnace or Heat Pump (Stage), AC and
HP high/low capacity commanded and some other related parameters.
This display is a touchscreen and settings are controlled by
touching the desired parameter (such as OCCupied) for a particular room
and turning it on or off. Setting individual room temperatures is
handled similarly or by individual room digital thermostats..

FIGURE 1 (above)
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A photo of the HI-Solutions model UUC-8 Controller Board is shown
below in figure 2. This board was substituted for the OEM Carrier Heat Pump
Controller. NOTICE:
The below UUC8 controller has been working beautifully with the Carrier
Infinity Heat pump now for over 5 years. Several people have
asked for and received assistance in implementing this same design in
their equipment. I was happy to assist. HOWEVER! This
is NOT a beginner's project. It is NOT for an EE who is
unfamiliar with basic HVAC technology and it is NOT for someone
expecting to do this project "on the cheap". The cost of the UUC8
board, the "maintenance kit" necessary to communicate and program the
UUC8, the differential pressure sensor, the EVO-EMC fan motor
interface and other incedentals will cost on the order of $700 to
$1000. If this would be your first programmable controller
project and/or you are not familiar with HVAC equipment, do not even
contemplate this project. That being said, if you are comfortable
with the above, I will be happy to discuss the project and assist in
getting the necessary parts. Joe Mehaffey

FIGURE 2 (above)
The following Figure 3 is not a typical day in the life of a heat pump
in heating mode, but it is a great show of how the new defrost
algorithm works in real life. Notice that the blue graph in the
temperature group is outside air temperature at the Heat Pump and the
green is outside humidity. The black graph in the Heat Pump Tons
group is heating Tons and the green graph is "stage number" for the
heating system. Stage 0 is OFF, Stage 2 is Heat Pump ON and Stage
3 is Heat Pump plus Auxiliary Gas heating. In the Total Amps
graph group, the RED graph is the differential pressure across the
Outside Evaporator/Condensor (VAC is in units of 100 times the
pressure difference in inches of water.), the black graph is is
the total amps drawn by the Heat Pump unit and the green graph
represents the Outisde Coil Refrigerant Exit Temperature
DIFFERENCE from the Outside Air Temperature.
Notice that the Outside air temperature was below 35F for much of the
night, rising to 40F only around 2PM. The outside humidity was about
97% during this entire interval. During this time, and beginning about
6AM when the heat pump begain running continuously for about 3.5 hours,
the Outside Coil began to "ice up". This is evidenced by the
increase in "VAC" from about 0.11 inches at 6:15AM to about 0.25
inches at 9:30AM. During this time, the coil was slowly freezing
up and the coil temperature was constantly below freezing. Thus,
the Carrier Defrost Algorithm would have defrosted about every hour
during this interval. The freezing conditions continued until 2PM
when the coil finally thaws out due to the warming temperature.
The important thing to note is that at no time during this 10 hours of
coil icing was a defrost cycle called by the new defrost algorithm
BECAUSE the pressure differential never got up to the trip point of
0.35 inches. The graphs of amps drawn, and Supply Air Temperature
(TSAT) indicate little if any capacity reduction during this
interval. We know that some capacity reduction occurred because
the DELT (Outiside Air minus Outside Coil Temperature) slowly rose from
about 6F to 10F during this interval. However my calculations are
that the very small reduction in capacity was MUCH less than the amount
of energy which would have been expended and lost by defrost cycles.
Not to mention the fact that while the equipment is defrosting,
it is not only not delivering HEAT to the building, but is, in fact,
delivering COLD into the structure! It is for these reasons that
the new defrost algorithm is an important improvement in Heat Pump
Operation.

FIGURE 3 (above)
Below is a typical graph of Heat Pump operation with outside air in the
range of 35F with the new algorithm. Note that the machine ran
for a full 12 hours in this instance without a single defrost cycle
being required. The VAC never got above about 0.13" in this
period because the outside humidity (HUMO) was less than 78% for the
entire interval. The pressure differential measurement across the
outside coil automatically takes this lower humidity into account
because the icing amount was less resulting in less pressure drop
through the coil. In the graph below, OAIR is outside air temp,
BTUH is computed Heat Pump capacity in the selected Low/High mode,
DELT is the outside evaporator coil temperature difference and
VAC is the pressure drop across the outside evaporator coil in inches x
100. (VAC=10 indicates 0.10" pressure drop across outside coil.),
TAMP is the total amps drawn by the fan and compressor in the
heat pump unit. Note: A defrost cycle occured when
TAMP shows the compressor is running and VAC is zero showing the
outside fan is NOT running as in figure 5 at about 8:50AM.

FIGURE 4 (above)
In the figure 4, note that over this 12 hour period where the
outside coil temperature was frequently below freezing for short
periods (and the Carrier algorithm would have run about 4 defrost
cycles), the new algorithm did not call for a defrost even once.
Note also that the pressure drop never got above about 0.12"
during the period and there was no drop off in TAMPs such as you see
with the capacity reduction which accompanies a freeze up situation.
This was a situation where there was a) medium humidity, and b)
the
normal heat pump shutoffs at frequent intervals allowed some defrosting
to occur at intervals without running a machine defrost cycle.
Another phenomena demonstrated by the above graph is the value of good
home insulation. Note that the Outside Air Temperature (OAIR) was
down to about 37F at 23:00hours. But the system continued its
cycling on/off at a pretty steady duty cycle until about 04:00 when you
notice the first transition of BTUH above the LOW capacity during the
night. Starting at 06:00 the system goes to high capacity and
stays there for 1.5 hours. Then at 08:00, the family room is
"turned on" and the system then runs in HIGH capacity for several more
hours. During this sequence, I locked out the auxiliary gas
heat so the overall effectiveness of the 48,000btu heat pump in the home (all rooms set to occupied) could be evaluated.
As shown in the graph, the actual heat pump output at 35F
outside was in the range of 37,000btu/h during the night.
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In figure 5 below, Notice that there was obviously increasing
icing of the
outside coil from about 6AM.. However the icing only got
the pressure drop
across the outside coil to 0.35" (red VAC graph line) at about
8:45AM and so there was only one defrost cycle during the entire night
with the temperature below 40F for the entire period. The OEM
carrier defrost algorithm would have caused a defrost cycle about four
times. It is interesting to note the DELT (green) curve in the
lower curves of figures 5 and 6. It can be seen that
when significant icing is occurring, the value of DELT stays POSITIVE
during the normal heat pump compressor OFF cycle. But if there
is no significant icing, the value of DELT reverses and goes negative
during the OFF cycle. This results because with little or no
icing, the small amount of heat left contained in remnants of the
refrigerant in the inside condenser coil moves outside to the
colder evaporator coil and is enough to heat up the outside coil
to above outside ambient temperatures between cycles unless
signifiant ice is present.

FIGURE 5 (above)
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The image in figure 6 below shows another night when the temperature
hovered around freezing. Note that from about 5AM the temperature
was around 35F and there was a lot of running of the heat pump from 6AM
until 9AM. Yet, not a single defrost cycle was requiested by the
new algorithm and none was needed. The OEM Carrier Algorithm
called for 3 defrost cycles during this interval. Note the
multiple momentary power failures at about 5:20AM. These had no
effect on the operation of the new algorithm. But the OEM Carrier Algorithm
would have reset the defrost timer to 30 minutes as a result of the
power fail and this would have perhaps generated a fourth defrost cycle
in the Carrier OEM defrost algorithm for this period.

FIGURE 6 (above)
The figure below shows a
sustained period when the outside temperature was between 33F and 38F.
The humidity was in the range of 70% so there was not as much
icing as you might expect in that temperature range. However,
between 6AM and we do see the red VAC curve arch up to a maximum
pressure drop of about 15 (0.15"). The graph shows that on this
day there was no defrost cycle called for. The OEM carrier
defrost cycle algorithm would have called for a defrost 2 or 3 times
during this interval. The BTUH curve shows that the system was
alternating between the low and high output modes in the 6AM to 8AM
period finally going to high output mode continuously at about 8:30AM.
At about 8:30am, there is a small "pip" on the STGW up to stage 3
and BTUH graphs indicating that, for a few minutes, auxiliary gas
heat was turned on.
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FIGURE 7 (above)
In Figure 8 (below) is shown
another near freezing night without even one defrost cycle being
called. The OEM algorithm would have called for 2 or 3 defrost
cycles during this interval. Note, that the upper group of graphs
has been changed to include Outside Humidity, Supply Air
Temperature as well as Outside Air Temperature. Again, note the
multiple changes from low to high heat pump capacity as shown in the
BTUH and TAMP graphs. The STGW graph should be ignored as my data collection equation was not operating properly.
FIGURE 8 (above)
In Figure 9 (below) we see a
night when the temperature went to freezing at about 4AM and stayed
there until about 9AM. Only one defrost cycle was called for and
that was at about 9:10AM when the air pressure drop across the outside
coil finally made it to 0.35". By comparison, the OEM Carrier
algorithm called for defrost three times.

FIGURE 9 (above)
Figure 10, below, shows Heat Pump operation on a day when the minimum
temperature was 20F and the maximum was 28F. Note that the
humidity on this day was below 80% and that NO DEFROST CYCLES were
required or run. During the night, the heat pump mostly ran in "low"
heating mode only going to "high" heat mode after 6AM as the living
quarters zones were turned on. Note also that the heat pump ran
continuously for more than 5 1/2 hours from 6:30AM without any
appreciable VAC pressure drop across the outside evaporator and was
producing between 2.5 and 3.0 tons (30,000 to 36,000BTH/h) of heating
during this period. The standard carrier algorithm a) would have
defrosted probably 4 times during this interval and would not have
allowed operation below about 32F. This is a dramatic showing of
the improvement in operation of the new heat pump defrost control
scheme. Note also the green curve of STGW. This shows that the
auxiliary heat (STGW=3) came on for only two short periods during the
night but it did run pretty continuously from 7:45am through 10:15am
adding 45,000btuh to the heat pump's 30,000+ BTU/h. Note also
that the 90,000BTU/h supplemental furnace (STGW=4) never came on line.

FIGURE 10 (above)
Figure 11 (below) shows a full
day of operation of the heat pump system with the temperatures ranging
from about 13F up to a high of 40F. Note that from the time
the temperature went below 20F the system switched over to the backup
(natural gas) furnaces. But except for that period from about 2AM
until 10AM the heat pump was running and almost continuously and
without any sign of a freezeup as shown by the VAC reading
staying in the normal range of just about .11" to .13". The
evidence is becoming pretty strong that whenever the humidity is below
about 80% or so, defrost cycles are seldom needed. Even above 80% RH,
the number of defrost cycles used by the Time+Temperature algorithm vs
the Pressure Difference used here is about 5 to 1. This is more
(and pretty conclusive) evidence that the time+temperature defrost
algorithm used by Carrier and most other manufacturers is causing MANY
MANY wasted defrost cycles. This graph Figure 11 also
demonstrates that the heat pump provides useful heat output of about
2.5 tons (30,000btu) all the way down to 20F. UNfortunately, in
this case, the amount of heat required to maintain "balance" at 20F is
about 80,000BTU/H and so at 20F the switch had to be made automatically
from the 30,000 BTU/H Heat Pump + 48,000 BTU/H NG to the 90,000BTU/H NG
+ the 48,000BTUH NG.

FIGURE 11 (above)
Figure 12 (below) shows
another interesting characteristic of the icing of the outside
evaporator. This scatter plot has data on Outside Humidity
as the Horizontal Axis and Intensity of occurances of VACuum
measurements (differential pressure across the outside air coil) on the
vertical axis. This data was accumulated over the period from mid
November to 5 January 2008. Notice that ALL of the
significant icing (as indicated by red dots above VAC= 12) of the
outside heat pump coil has occurred when the outside
HUMIDITY was greater than 85%. Below this humidity level, no
significant icing occurred at any outside air temperature between
20F and 40F. During this period, the heat pump was run for up to
6 hours continuously in temperatures from 20F to 40F. I
consider this factor very significant as it is another measuranble
parameter that could be used in a decision process as to when
defrosting of the Heat Pump outside coil is necessary. This is
vivid evidence that the current time+temperature algorithms are causing
the World's Heat Pumps to enter the defrost cycle FAR too frequently.

FIGURE 12 (above)
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